移动床生物膜反应器
反硝化
硫黄
化学
水力停留时间
废水
污水处理
氧化剂
渗滤液
硫代硫酸盐
硫化物
硝酸盐
氮气
环境化学
制浆造纸工业
环境工程
废物管理
生物膜
环境科学
细菌
有机化学
工程类
生物
遗传学
作者
Yan-Xiang Cui,Di Wu,Hamish R. Mackey,Ho-Kwong Chui,Guanghao Chen
摘要
Sulfur-oxidizing autotrophic denitrification (SO-AD) was investigated in a laboratory-scale moving-bed biofilm reactor (MBBR) at a sewage temperature of 22 °C. A synthetic wastewater with nitrate, sulfide and thiosulfate was fed into the MBBR. After 20 days' acclimation, the reduced sulfur compounds were completely oxidized and nitrogen removal efficiency achieved up to 82%. The operation proceeded to examine the denitrification by decreasing hydraulic retention time (HRT) from 12 to 4 h in stages. At steady state, this laboratory-scale SO-AD MBBR achieved the nitrogen removal efficiency of 94% at the volumetric loading rate of 0.18 kg N·(mreactor3·d)-1. The biofilm formation was examined periodically: the attached volatile solids (AVS) gradually increased corresponding to the decrease of HRT and stabilized at about 1,300 mg AVS·Lreactor-1 at steady state. This study demonstrated that without adding external organic carbon, SO-AD can be successfully applied in moving-bed carriers. The application of SO-AD MBBR has shown the potential for sulfur-containing industrial wastewater treatment, brackish wastewater treatment and the upgrading of the activated sludge system. Moreover, the study provides direct design information for the full-scale MBBR application of the sulfur-cycle based SANI process.
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